MK5 Golf GTI
All Things Mk5 => Mk5 General Area => Topic started by: v4rley on October 29, 2017, 09:11:22 pm
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After visiting R-tech I left no better due to the car not being able to achieve requested boost. The actual is a consistent 4psi below:
(https://www.mk5golfgti.co.uk/forum/proxy.php?request=http%3A%2F%2Fi68.tinypic.com%2F2hp6e08.png&hash=0a5f5e645bbce21ddd4cb95ef088081e94238b98)
The car was smoke tested on the day and a good going over by the team there.
I’m left trying to figure out the issue. Would this appear to be turbo problem?
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Only 2 possibilities - 1) the boost is bleeding off, or 2) it's not making any boost. 1) is most likely. PCV, DV, boost hoses leaking..... the usual checks to perform.
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Weak actuator is another - Sure i saw another thread of yours with VCDS graphs in showing 100% N75DC..... So either your turbo is broken, you have a leak, or your actuator isn't doing its job.... As the requests certainly weren't unreasonable for a K03 from memory
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@Pudding (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=10733) It was smoke tested on the day at rtech and also did some smoke test whilst on the dyno so not sure if there is still an unditected leak
@Dan_FR (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=9513) yeah they were my logs.
Brief history of the car I have had it for 5 year, already had a stage one quantum when i got it. Mainly the wife’s car but I occasionally give it a good drive now and again. On this map it was running 95% N75. Maybe to my perral I have had the bcs and intake in for the last two year on the original map and on WOT it would have black smoke when the boost kicked in.
Niki said the actuator wasn’t the sloppiest he had seem but obviously this was only a manual check from under the car with a bar reaching up in. Other suggestions was that the tips on the turbo have melted
I have only just got my head around logging so haven’t got any earlier ones to compare to. I find it strange that the boost seems to follow with a consistent -4psi
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Did Niki actually confirm there is an issue? Did he not map it or just upload a base map? Did he give any advice or suggestions?
Turbine tips can be examined by removing the downpipe, compressor side can be examined with a cheap borescope. If you dont have a boost leak, and are running at 100%DC and not making the boost (and airflow - MAF reading?) then it can only be some form of turbo problem. Extra preload on the actuator can help rule that out, so probably worth trying
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Yes he said it was the worst he had ever seen and left with a addition 2hp from the original map.
His first concern was that I had installed DV relocation kit (k04 style) same as here (http://www.mk5golfgti.co.uk/forum/index.php?topic=17736.0) Say that he had never seen it done before. So he suggested I started by putting back to oem (which I have) and still logs the same. He did spend some time looking at various aspects and trying to sort it but obviously limited time available.
He has loaded the 5 map thing and these log are in #5 so haven’t logged or know what the N75 request is on the others.
Ok haven’t logged the MAF will do that on my next logging session, would this have been looked at whilst mapping ?
To add preload I guess that’s adjusting the bolts on the actuator rod is that feasible with it still on the car?
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Assuming the DV and boost plumbing is all good; Test the PCV, check the rear breather tube for cracks as well as fitment to the turbo (also the anti reverse flow valve inside), check the Mass air data (full load 2k rpm to redline...2nd gear is OK), and post the values of 'LTFT group 032 blocks 1 and 2' (done while idling when fully warmed).
Check the N75...one of the three nipples could be cracked or have loose hoses attached.
The WG preload is likely not what's failed...but not one to rule out just yet.
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Block 032 after above logs were done
(https://www.mk5golfgti.co.uk/forum/proxy.php?request=http%3A%2F%2Fi64.tinypic.com%2F334rbwx.jpg&hash=76d5582660b2f5f0191d0f2629d25168dab4a4ec)
Checked the N75 all seem fine with no damage to nipples and still oem clips intact and firm
Dv and pipework appear fine
Rear pcv again doesn’t seem to be crack or any damage
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This all is looking like the wastegate. Likely not sealing when wgdc is near maximum...due to WG not sealing because damaged or there's loose linkage allowing slop in the WG positioning.
Nothing points towards leaks in the LTFT. It runs a bit rich...below 0.82 actual is a bit rich and LTFT multiplicative also confirms richness at -1.6% additive. Low pressure pump dips below the 4 bar minimum.
It is not common for the WG actuator diaphragm to tear...but the spring inside the actuator may have weakened. You may try adding WG preload, but it is tough doing on a K03 vs a K04...but can be done. Look up vids on how to change WG preload for guidance or I can help with questions. The thing is, is if you do make an adjustment and find it getting better...likely would want to start thinking about removing the turbo and give it a thorough inspection and possibly end up replacing the WG actuator. So, might as well be prepared for a new turbo with actuator included.
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There is a adding preload guide (http://www.golfmk5.com/forums/showthread.php?t=23337&highlight=wastegate) So basically this is what I need to attempt
I did acquire a second hand k03 the other day as it was on my travels as I can have a good look at that in the garage before attempting the one on the car.
The fuelling situation would the be a situation as this is only a base map so hasn’t been fine turned for optimum efficiency?
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The drop in the low pressure side coincides with the high pressure side creeping to 140bar - unsure why the car is doing this but certainly is not the issue. Everything else looks good, load, MAF looks bang on too for a K03 etc.
If it were my car, the next thing I would do personally is remove the vacuum pipe to the actuator and take it for a drive, with the laptop on and keeping a VERY close eye on the boost reading. In theory it should drive exactly the same in terms of peak boost and performance, but there's a chance it could not and you could see turbo shattering boost levels at lower rpm
I'd also go with checking the wheels for any damage, melted tips etc. as its fairly easy to do, and if they look OK and the pipe removal yielded no significant change, I'd re-attach it and then add a fair bit of preload to try it out and see how you get on - you can always back it off at a later date if its a little much
19PSI peak with 100% N75DC (based on previous graph/log), without a leak, is definitely a turbo problem. This little turbo could easily peak at over the MAP sensor limit of 1.5Bar by 3k RPM if all were ok
Also, just an FYI - my K03 2+ can hit and maintain the requested boost levels in this map, so they are achievable and are what you should be aiming for
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OK, thanks I truly appreciate that assistance from you both and will do as advised. I’m a long way from rtech and no Indy’s near me so this help it great :notworthy:
So tonight’s plan is to remove the actuator boost feed and see what is achieved. Would I be ok montering this is polar fsi? Just a bit easier to do whilst driving.
I have just ordered a borescope so will get onto this once it has arrive.
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Has the turbo whistle pitch changed recently? That's how on a previous car I knew something was up with it. The whistle changed in volume and pitch.
It drove OK though, but when I inspected it, all of the inducer blades on the compressor wheel were chewed to pieces. Obviously something harder than aluminum made it's way through the intake! Bye bye 1 x expensive GT3071R turbo :doh: Niki posted a pic on the TFSI group ages ago of the exact same thing on a MK6 R that wouldn't make the usual power........but people love their plant pot on the end of a pipe intakes don't they.
As per Dan, god knows what that HPFP spike is all about (EGT / component protection map kicking in perhaps), but you are running some crazy AFRs. Mid 11s in places. Waaaaaaaay to rich for DI. ~12.8 is where it needs to be, otherwise it defeats the purpose of DI. Mid 11s is old port injection nonsense because tuners were too afraid to tune for power. No need for that at all on TFSIs.
Anyway, I'm not convinced it's an actuator problem. I think the turbo is worn out / damaged personally, but keep us posted!
P.S. What app do you use to make those nice graphs from the VCDS logs?
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Haven’t really noticed a difference in turbo noise, have tried a few dire things intakes over the years so alway getting different tones anyway, I haven’t experienced any loss in power either.
As mentioned earlier thing is I don’t often drive the car and usually with the family when I do so not often it gets driven hard, maybe this has prolonged the issue turbo life
Yeah I have know idea about fuel trims / afr Niki did say about over fuelling may have cause the turbo to overheat and damaged the fins.
Ah the logs! They are with thanks to @dazza (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=10457) for writing the program to do the graphs, although it took me a while how to figure out how to use it! guide here (http://www.mk5golfgti.co.uk/forum/index.php/topic,88889.0.html)
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Good to see you're on track to narrowing down the issue! You've got some great help - sure you'll get it sorted.
Pudding - gutted about the turbo! Im assuming from your plant pot intake comment you run a standard airbox - which has a gauze either before or after the MAF so essentially two safeguards for stuff entering the turbo.
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Ah the logs! They are with thanks to @dazza (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=10457) for writing the program to do the graphs, although it took me a while how to figure out how to use it! guide here (http://www.mk5golfgti.co.uk/forum/index.php/topic,88889.0.html)
Glad to see this feature being used it took a while to build that.
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Ah the logs! They are with thanks to @dazza (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=10457) for writing the program to do the graphs, although it took me a while how to figure out how to use it! guide here (http://www.mk5golfgti.co.uk/forum/index.php/topic,88889.0.html)
Glad to see this feature being used it took a while to build that.
Its brilliant - I use it a lot. I just edit and save the existing posts, as I dont want to clutter up peoples "new posts" with long posts
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For when you go and add preload...once car is raised and secured, remove the heat shield about the right axle. Remove the rod clip(1) with a flat driver. With a 10mm open-end wrench/spanner, loosen the 10mm nut(2) towards the actuator diaphragm. Probably want 2 to 3 full turns to see if a difference is made...so, count the six sides as you turn the nut. Then turn the knurled nut(3) the same direction until it is snug with the 10mm nut and tighten using the 10mm nut. Replace the rod clip and heat shield.
(https://farm5.staticflickr.com/4231/35574442181_e5c8cc0eff.jpg) (https://flic.kr/p/WcAjgp)
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Ok so tonight’s logs are as follows below, this is with the vacuum feed for the actuator removed (just let dangeling) again still not reaching the requested so does this rule out the wastegate?
So next steps will be to inspect the wheels for damage, and then having a go with preload unless that is now obsolete with tonight’s results?
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Rules out the N75 and boost control system/plumbing etc.
Wheel inspection and preload next
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Ok thanks. Going to save the preload for daytime job for more assistance with daylight so will likely be Saturday due to work commitments. Borescope should be here by the end of the week. So that’s my next tasks sorted. If there is anything in the mean time to investigate / diagnose let me know
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:thinking:
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Good to see you're on track to narrowing down the issue! You've got some great help - sure you'll get it sorted.
Pudding - gutted about the turbo! Im assuming from your plant pot intake comment you run a standard airbox - which has a gauze either before or after the MAF so essentially two safeguards for stuff entering the turbo.
I do indeed. The gauze is before the MAF and it's just to straighten the airflow for accurate readings, I doubt it would stop a stone or a flicked up nail or something. There is no way anything would find it's way through the labyrinth of the OEM airbox. I think what happened with my GT3071R was something small got sucked through the cotton gauze and took out the inducer blades. It sounds far fetched, but if hold up a cotton pleat filter to the sky, you can clearly see daylight through it. Every time I've used cotton, both the MAF and impeller blades have been filthy compared to paper.....it's a ticking time bomb.
Cotton is crap. Foam or paper. Paper is way too tight to get anything through it, and foam is very dense and would trap a piece of grit like fly paper.
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You've got some beefy timing pull going on there V4rley. The old girl is not happy. The timing is low in boost as it is, plus that amount of retard and 11.5 AFRs......christ yeah that is going to super heat the turbine blades. And wreck any cat converters in the vicinity.
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Yeah this data stuff is a bit technical for me but didn’t think the cylinder graph looked great :sad1: I guess this need mapping to sort? as apposed self sorting once the boost issue is sorted?
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The timing will sort itself out if everything else is happy
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Yeah this data stuff is a bit technical for me but didn’t think the cylinder graph looked great :sad1: I guess this need mapping to sort? as apposed self sorting once the boost issue is sorted?
What map is on it currently? Quantum? I've not heard of that. Is it a switchable map allowing you to load a 'stock like' map?
I'm just conscious it might be a wasted day going to R-Tech with these issues because it might not be software related. It rarely is. A map is a map. The hardware is usually always obedient to commands, so long as they are not pushed too far.
How far is Hinckley from you? If it's a fair distance, I would be tempted to get your VW dealer to wipe the ECU and reflash it with the OEM map. Then repeat the logging and see if things fall back to where they are supposed to be. Do a compression test as well, and check all the sensors etc, including the cam sensor which can get covered in sward, and then the ECU runs the 'rough running' map.
Personally, I would only go for a dyno map knowing my engine is 100%. It saves your time and money, and their's too. As I said previously, no mapper can fix hardware problems with software. They can attempt to work around them, but it's just a band aid. A reflash back to stock will confirm the hardware is good or bad.....but it'll cost you an hour's labour. That might be cheaper than having Niki troubleshoot it all day.
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Currently has Rtech with the 5 switchable maps.
After arriving at rtech for a noon booking it appeared that I had somehow arrived in big turbo week, so wasn’t idea for them. But they got straight on it, Niki didn’t like the dv relocation one bit and got a bit of a negative vibe. But after a couple more hours of playing with leak testing, strong dv springs time was up and i had the family with me towards the end so I had to get on and depart swiftly at 5pm.
My brief understanding is that the maps get progressively more ‘agressive’ he said to go with 5 as not much to loose as demands not being furfilled anyway. I will speak to him more specific but wanted to try and source the problem before hassling him as to make the most of a call.
It’s some distance away at 200mls and a ferry :sad1:
Perhaps whilst awaiting the weekend events I should do a quick log on map 1 to see what the difference is? Which of these APR logs (http://www.goapr.co.uk/support/datalogging.php) would give the best insight?
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Ah OK, I must have missed the bit where you mentioned it was R-Tech'd already.
Yeah you could try a logging session with the least aggressive map. Map 1 should be the same as standard. Most tuners use a 'stock like' map and not the actual code VW uploaded to the ECU, so it may not drive exactly like a standard car.
VCDS can only log up to 12 channels at once iirc, so we can drop the ignition retard channels for the stock like map, so go with:
Engine speed
Lambda regulator (current value)
Lambda - req
Lambda - act
throttle plate angle
Pedal angle
high pressure fuel - req
high pressure fuel - act
Boost - req
Boost - actu
Intake temp
MAF
Give that a whirl and see what you get!
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4 maps original
Ok I didn’t choose the best measuring block but hey some are ok. Interesting one I think is the boost let me know what it means 😂
Ok so the graphs are grouped, there are 4 runs. Map 1 then 1 then 3 then 5 (as all previous logging)
Sure you guys know but buy clicking on the point on the graph it tells you the value at that point as my first rpm and maf combo doesn’t work well together
Map 1 run 1
Map1 run 2
Map 3
Map5
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The boost and HPFP graphs are weird!!
If you go to Engine > Advanced ID in VCDS, what numbers do you have showing for Flash attempts and successful flash attempts? Just wondering if your ECU is corrupted.
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@Dan_FR (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=9513) @Pudding (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=10733) @ROH ECHT (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=3794)
(https://www.mk5golfgti.co.uk/forum/proxy.php?request=http%3A%2F%2Fi68.tinypic.com%2F6r6m34.jpg&hash=b2bf8d1abb123b0b54744bb854745e38491fcdf2)
(https://www.mk5golfgti.co.uk/forum/proxy.php?request=http%3A%2F%2Fi68.tinypic.com%2Fxeokug.jpg&hash=9da0dc3cc3925e19f6f25c92a2d4f97bf3b06bdd)
(https://www.mk5golfgti.co.uk/forum/proxy.php?request=http%3A%2F%2Fi65.tinypic.com%2F2v1ueci.jpg&hash=3f8805bafc5b6444dab037a6deb44a8a06793cde)
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@Pudding (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=10733)
(https://www.mk5golfgti.co.uk/forum/proxy.php?request=http%3A%2F%2Fi64.tinypic.com%2F2v92dk4.jpg&hash=1cd542ec4cabe8cfa8b5fa6215e4c7a3680bd2b2)
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Ok sound wound the actuator on 3 full turns of the hex nut, below are the logs definitely the best peak figure so far but not sure if it runs out of poof sooner
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There doesn't appear to be any turbo damage looking at those pics. What borescope did you use? The image quality is pretty good. Did you drop the probe in through the lambda port on the exhaust side, or did you remove the downpipe? Just wondering if you spun the turbo by hand to see if there was much shaft play?
Maybe the boost is lower because the engine isn't running optimally? Just thinking cylinder 4 is not happy at all with all that ignition pull. Perhaps you have a bad injector and it's running lean. The onset of boost is sluggish as well as not hitting the requests....... I think get the ignition pull sorted and it might return back to normal health.
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That turbo looks pretty good to me. Did you spin it to make sure the bearing doesn't feel rough/uneven or have an abnormal amount of resistance and/or play?
As for the timing pull, have you actually logged how much timing you are running at the same time so we can see how much timing you're actually getting? Can't say I've seen it in any of the logs? I don't think the timing pull is the cause of the turbo or performance issue at all. The throttle isn't closing so the car isn't THAT unhappy. I've personally seen that level of timing pull during some logging/testing/tweaking of Revo software on my own car and it most definitely did not pull back boost levels as a result
Would have expected the actuator tweak to help a lot more if it was the cause of the problem.
Silly question, but have you checked to see if you have the correct MAP sensor fitted to the car? Your MAF values are good, and you say there's no leak, so I'm wondering if the wrong sensor is fitted.... a 3 Bar sensor fitted to a 2.5 bar calibration will make the ECU see lower boost than you actually have..
E.G. You could see several hundred mbar difference between the two sensors. Don't suppose you have an aftermarket gauge plumbed in to the inlet manifold?
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If the cylinder is delaying the burn and thusly the cylinder pressure / contribution drops, flow through the engine is reduced and that includes exhaust flow over the turbine wheel, no?
That amount of pull is not good. I get -2 KW at the most running a lot more boost than that. I'd be looking to get that as close to zero as possible before going any further.....personally.
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Negligible effect on boost levels and wouldn't cause a 4 PSI deficit across the RPM range - based on my own experience with a K03. Besides, looking at the log, the knock level is not constant and it is peaking, most likely at a certain load/RPM so wouldn't explain the drop across the entire rev range
The amount of correction is based on the severity of the knock detected and will depend entirely on the requested ignition timing - its not comparable on different cars & setups. Its not ideal but the ECU can deal with up to 12CF so its not an issue for the purposes of this diagnosis. At 2CF you probably have no real knocking going on and you may not even have any reduction in timing, its just a Correction Factor and does not directly translate to X amount of degrees of timing retardation
Anything up to 5CF for short periods is fine anyway based on what I have seen over the years from many logs and heard from tuners themselves, 2CF at most tells me you have a safe map with headroom for more, but again it depends on a lot - ambient conditions, whether your 2CF peak was after a single run or after repeated back to back runs for maximum heat etc.
Off topic a little, sorry! :signLOL:
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Yeah the turbo looked good to me, part of me was hoping to see issue to resolve the problem but alas not. Just the standard cheap borescope from eBay pretty good although the mirror angle bit is crap.
I cheated and use the lambda for the exhaust side, did consider removing the downpipe for inspecting the play maybe something to consider. With regards to the play i have a k03 in the garage, when I put the airline into the cold side it spun the wheels but when I replicate this on the car it didn’t, although not sure if that is just due to the resistance from the one on the car having oil / coolant amounts it.
All my logs are on this thread so haven’t got the timing ones. Can you point me in the direction of which measuring blocks and I’ll log them tonight.
I had a rare misfire issue months ago, mainly at low speed and usually over speed bump, this was cylinder 4 and maybe also 2. The injectors were replaced with a freshly cleaned set prior to mapping
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003-4 is ignition timing, I refer to this all the time for logging addresses http://www.goapr.co.uk/support/datalogging.php
I don't think it is relevant at all to the problem you are having
Not comparable on the car as the turbo may no be able to spin as the TB will be shut so the air has nowhere to go unfortunately.
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Ok so I need to check the map sensor, what would be the next avenue to try? Would you try more preload?
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Do you know why on these logs showing differently map setting, alway request the maximum but the actual boost seems to be map specific? (https://www.mk5golfgti.co.uk/forum/proxy.php?request=http%3A%2F%2Fi63.tinypic.com%2F35lf6o7.jpg&hash=e15e6a24905a19fb65d848cb220f34b0e222f42c)
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Its the way Niki sets up the switchable mapping, its done via the N75DC request rather than what will show on VCDS under 'specified'....
But the specified shown is achievable on a K03 on 100%DC. Mine peaks at around 1.3-1.4 bar and tails off to 0.8-0.9 bar at the redline
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Ah ok thanks makes sense,
So on the latest set of boost logs (after preload tweak) my peak is the same / higher than yours but is a good 3-4psi lower at the redline.
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Negligible effect on boost levels and wouldn't cause a 4 PSI deficit across the RPM range - based on my own experience with a K03. Besides, looking at the log, the knock level is not constant and it is peaking, most likely at a certain load/RPM so wouldn't explain the drop across the entire rev range
The amount of correction is based on the severity of the knock detected and will depend entirely on the requested ignition timing - its not comparable on different cars & setups. Its not ideal but the ECU can deal with up to 12CF so its not an issue for the purposes of this diagnosis. At 2CF you probably have no real knocking going on and you may not even have any reduction in timing, its just a Correction Factor and does not directly translate to X amount of degrees of timing retardation
Anything up to 5CF for short periods is fine anyway based on what I have seen over the years from many logs and heard from tuners themselves, 2CF at most tells me you have a safe map with headroom for more, but again it depends on a lot - ambient conditions, whether your 2CF peak was after a single run or after repeated back to back runs for maximum heat etc.
Off topic a little, sorry! :signLOL:
Aye, I was just concerned that amount of knock isn't healthy in the peak cylinder pressure zone. 'CF' was more ME7. Timing delayed in .75 degree chunks every XX crank rotations until it stopped. MED9 is different. The KW shown in the knock regulation activity is the actual degrees pulled.
Anyway, it seems like the hardware is good, which was the initial concern.
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MAP sensor is 038906051D so looks to be 2.5bar one
Will do some logs later, anything else to try / investigate?
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Timing retardation looks a little less on that one, probably because the IATs are colder now.
I find the graphs a bit hard to read without rpm or load on the horizontal axis!
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@Pudding (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=10733) Yes does look a bit happier this time.
Understand about the lack of rpm on the graph, not sure if I’m not including in the log or the way it’s programmed @dazza (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=10457)
Any suggestions what to try next?
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Not sure mate. Apart from the timing pull and strange HPFP spikes, nothing really jumps out as a massive concern.
I'm guessing all the dips are you changing gear / slowing down?
Ideally, a nice 10 second burst of full throttle in 4th would be good to see if everything matches the targets, but it's not always doable on the roads!
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The logs are all 3rd pulls from 1.5k to redline. I know it’s not ideal graphing but if you look at the top rpm graph it follows down through the other graphs, ie the peak in the rpm graph aligns down the page with rail pressure etc.
Ok I am great full for the help from everyone and appreciate its a limited being diagonosed over a forum but just try to ensure I have exhausted all possible avenues.
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Ah OK, so in the G79 Pedal position graph above, that dip down to ~50% wasn't you letting off? If not, that isn't good. Would be interesting to see if the throttle position mirrors that dip.
Yeah internet diagnosis is tricky!
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Wish I could help on something like this! I haven't the foggiest though, wish it was something simple as just "change the DV"
Legends Dan and Pud will see this sorted hopefully!
Good luck James mate
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I too thought the dip was V4rley letting off the accelerator before going back on it- almost like two separate runs.
Is it infact that the above graphs are of one, constant pull?
Is it worth noting that lambda stays at 0.8ish throughout the pull, it doesnt rise up back to one (as would be expected if letting off the throttle)
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It depends if the throttle closed 50% as well, and also how quick that blip was. At WOT and high rpm where everything happens so fast, lambda is notoriously poor at detecting transients, and is also too slow at making fuel trims at those rpms. It is for that reason a lot of high performance engines switch to open loop under high load / rpm conditions. I would say if Varley didn't feel that dip, lambda sure as hell wouldn't have 'seen' it either.
We might have to resort to reading the data row by row in Excel......which I hate.....so Dan can do it :grin:
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Hmm, cannot recall the exact even at the dip, it was a 3rd pull and changed into 4th (dsg so no lift off) but on limited open road and high in the 4th hear rev range I could have hesitated and momentarily lifted off.
Thanks for the kind words @MIJ_JAGGER (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=16715)
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Ah....if it's DSG, I think it does momentarily cut the engine torque during a shift, not that end users feel it. Sorry, I was diagnosing with a manual gearbox in mind.
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Another thought.......have you got uprated engine mounts? Some really harsh ones have been known to fool the knock sensors into thinking there's detonation occurring, when there isn't. Just throwing that out there. Soft engine mounts do more than just make it comfy in the cabin :happy2:
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6 psi! I wouldn't get out of bed for that! I assume that is map 1, the 'stock like' map? Even stock pulls 10psi minimum, so that's odd.
I'm losing track of all this. In your other thread it seemed like you were getting there with the boost targeting and the graphs were looking good?
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Yeah the 6psi was crazily slow :grin:
So yeah it’s all got a bit muddled with different graphs, these are bumped from inside this thread as I’m trying to tidy up the graphs a bit now I can sort rpm out.
but yes we are getting somewhere, once I have the preload wound off a bit tonight, I’ll get some nice new graphs loaded :happy2:
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MAP 5
MAP 3
MAP 1
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MAP 5
Logged map 5 to show fuel pressure
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@Dan_FR (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=9513) @Pudding (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=10733)
These are back to back runs all 4th gear
Ok, so do you think I should tweak the preload to achieve nearer 22psi peak on map 5?
Fuel pressure is still peaking high but this I guess is down to the RS4 valve.
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Question is:
Do you want to get it set up perfectly for the current map as it is now with a flat 100% Dc, or get it set up to what will be ideal for when you go back?
For now, I think maybe you've gone a little bit too far back, but you're certainly not far away. Before going back to R-Tech I'd be either finding a new actuator or whacking on another turn or so of preload so you have all the boost available you could need, and Niki can manage the low RPM boost spike by fettling the N75 map for the higher map settings
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I didn't go back to page 2 when I last posted, but I still see it isn't fixed yet.
I just recently helped another having his WGDC remain at full capacity. He made adjustments adding preload and he too got close. But, I asked him to check his PCV and all its tubing as well. He found that his rear breather tube wasn't completely tightened to the turbo inlet. Once he fixed that, he had to lessen the preload again and the WGDC returned to normal operation. I may have said all of this before, but going to repeat myself if so.
It may be a good idea to check the PCV(if running one) and all the connections from the intake manifold to the turbo. If nothing is found there...give the boost plumbing another going over and inspect all its connections. DV is good I assume? I do not think you have a bad N75 or connections to and from it. It seems more related to an improper connection somewhere.
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I was thinking a thorough check over of the boost plumbing wouldn't go amiss too. The boost pipe O rings are an old favourite for bleeding off boost when worn.
That fuel rail spike is weird on map 5. I don't think that is the cause of the spike but something is forcing it to exceed it's 136 bar crack pressure, it relives the rail pressure then tries to go back up there again before the limiter kicks in, which seems to correspond with the momentary lean off on the lambda past 6000. Odd.
There's still a lot of ignition retard going on, even on map 1, which shouldn't be there at this time of year!
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Thanks guys.
@Dan_FR (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=9513) I was thinking to get it to peak around 22psi on map 5 so it is reaching its full potential them maybe running the car on map 4 until I was to revisit niki. So will add a bit of preload tonight
@ROH ECHT (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=3794) did wonder where you had got to. I will double check the pcv, everything was check at the time of mapping so confident they gave everything a good check and there hasn’t be deterioration since, but I will check this all again, assuming it can only be physically checked as not sure on pressure testing methods.
@Pudding (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=10733) as above all plumbing was checked at rtech and again since my return, I will take another look to confirm.
Don’t really get the fuel issue, does this present a problem?
Any thing to investigate/ inspect for the ignition retard ?
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The Map 1 log above is fine, the timing pull shown is part throttle no load when the engine is running maximum timing for fuel efficiency. As soon as you hit boost it disappears. No concern here at all
The fuel spike is explained if you are DSG - Its normal with an R-Tech map when approaching a gearshift, has been explained before.
The only difference between map 3 and 5 is the N75 map controlling turbo pressure - everything else including the timing requests are the same. The Map 3 log above with shed loads of preload is seeing the boost and airflow levels we are aiming for in Map 5 so the level of correction and timing pull isn't a concern in my mind.
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Thanks Dan. I will sort out some more preload tonight and general inspection of pipework.
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Maybe K03s are different but my K04 doesn't retard the ignition at all outside of the base timing map. And there is load at 1500rpm. If I floor it at 1500 in mine, manifold pressure shoots right up. Low vehicle speed and high load = a high probability of detonation, it's nothing to do with 'efficiency'.
Seems strange to request more rail pressure than the stock FRPV can handle, but what evs......if that's an R-Tech/DSG thing, fair enough.
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Those ones look a bit etcha-sketch!
Do R-Tech keep copies of customer's maps on their computer? If they do, I'd be tempted to get it flashed back to stock and repeat the tests, personally......just to outrule any hardware shenanigans. Flashed back to stock properly, as in at a dealer with their ODIS interface. Wipe the slate clean. The 'stock' maps tuners user aren't stock at all, but some low boost variation of it......probably pulled off a website like NefMofo.
If you still see the same issues, you need to sort them before getting R-Tech to bung the map back on. I think at the moment there's a lot of variables and reverting back to stock removes the software element out of the troubleshooting.
Having said that, things aren't looking horrendous by any means. Just more timing pull than usual and boost a little shy of requested.
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The second and third go wonky at the end due to loss of traction as was raining. Perhaps I should message Niki and get his opinion.
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Probably for the best. Internet diagnosis is challenging at the best of times.
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Yes for sure. But the help and guidance provided here has been invaluable and I thank you all for that :notworthy:
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We try :smiley: Not sure we achieved much though!
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R-Tech don't keep the maps, but that being said I thought this was just the basic Stage 2+ calibration on this with no fine tuning due to the issues you had with boost?
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Yeah that’s correct Dan basic map with the power achieveing tweaks.
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Thanks guys.
@Dan_FR (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=9513) I was thinking to get it to peak around 22psi on map 5 so it is reaching its full potential them maybe running the car on map 4 until I was to revisit niki. So will add a bit of preload tonight
@ROH ECHT (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=3794) did wonder where you had got to. I will double check the pcv, everything was check at the time of mapping so confident they gave everything a good check and there hasn’t be deterioration since, but I will check this all again, assuming it can only be physically checked as not sure on pressure testing methods.
@Pudding (http://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=10733) as above all plumbing was checked at rtech and again since my return, I will take another look to confirm.
Don’t really get the fuel issue, does this present a problem?
Any thing to investigate/ inspect for the ignition retard ?
Have you replaced the knock sensors ever?(http://cdn4.pelicanparts.com/techarticles/Volkswagen_Golf_GTI_Mk_V/48-ENGINE-Knock_Sensors_Replacement/images_small/pic01.jpg)
This is one thing that can, when failing to provide an accurate signal to the ECU, cause the ECU to pull more timing and reduce boost. Something to research if the air/boost leakage search fails to find fault. I would seriously consider replacing if nothing comes of searching and testing. They could be partially failing but not enough to code yet.
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You cannot log that way as them oem boost maps are not used the are redundant they could all be set to zero and have not bearing on the boost. The ecu us setup with rtech added code which is custom and custom set with every tuning session on the dyno unique to each car. As we said on the day your need to investigate the issues with actuator try find a strong health one and fit it this will take the boost up on all 5 map settings. Once the car is running a healthy actuator then you will need to come back to have all 5 maps setup around the new pre load to write a new boost profile this boost profile will be graphed and then you will have an actual custom boost profile to work from. Get the cars hardware fit first so the car can physically mechanically have the potential to make boost to support the custom mapping session. This issue was evident on the old map you had on the ecu which was 100% flat out
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you was told on the day after the first run with the old map that the n75 was flat out and the waste gate spring was the dictator of the boost something which limits what the software can over come, so there was a huge chance tuning the car would end up with the identical power which from memory it did? so the next step was to look into why its not mechanically making boost, i said add pre load and log if the actaul boost is higher by a small amount the you will need to get a new actuator fitted, or find a full healthy turbo, then run the car on map 1 then bring it back to have it fully setup to the new turbo or actuator, unfortunately the software cannot over come physical restrictions and magic up more boost / power.
This is way we tell every customer to log and get a full health check on there car prior to booking a mapping session, if you logged it prior and saw the turbo was flat out and still not hitting decent boost / power we could have looked at the logs and told you its a waste of time coming in for a map as you wont be getting a massive hike in power.
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I agree with ↑ tune not helping create boost when it is not already doing so as it should.
It has to be a component failing or loss of boost/air issue. I missed "how you tested the WG" as mentioned but you should have adjusted and added preload to see if there was any increase. If you do/did see an increase but still failing to match target boost...you need to find why. If you do not do so yourself and instead take it to a shop, they may not investigate as thoroughly as one needs to to locate the cause.
When the N75 fails, most of the time actual boost doesn't make target, drops very low, and then climbs a bit. WGDC usually looks normal though.
When WGDC is always at a high target, it usually means a loss of boost or air somewhere. Not common it is the WG actuator diaphragm...which can be tested for a tear by adding pressure and holding it while checking if pressure is lost using a gauge.
Checking for leaks or loose seals; intake to throttle body and intake manifold to turbo inlet; requires smoke or pressure testing. Some sections may need to be plugged at opposite end of point of inducing smoke or pressure.
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Ok so to keep everything update, obviously spoke to Niki and he kindly provided the above info, i couldn’t remember such a in-depth conversation about the preload but this does appear to be the issue.
Weighing up options, a new actuator is £130 plus needing to remove the turbo to fit. I have a borgwarner k04 in the garage that’s brand new so thinking if I got to remove the turbo anyway I might as well go for it. Atleast I will then know it’s a new complete new turbo unit.
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Yeah slap the KO4 on :happy2:
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Ok so to keep everything update, obviously spoke to Niki and he kindly provided the above info, i couldn’t remember such a in-depth conversation about the preload but this does appear to be the issue.
Weighing up options, a new actuator is £130 plus needing to remove the turbo to fit. I have a borgwarner k04 in the garage that’s brand new so thinking if I got to remove the turbo anyway I might as well go for it. Atleast I will then know it’s a new complete new turbo unit.
Just to add...The guy I mentioned having a loose rear breather and it fixed his issue...well, recently he went to a big turbo. He was having an issue again with boost. WGDC was always near 92% and boost would not meet the target boost. He found that the WG actuator provided with his turbo had a weak spring in it. This is when adding more preload will do absolutely nothing more...as the Actuator spring is allowing the WG to open prematurely. I wonder if you ever resolved this and what was found to be the fix.
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@ROH ECHT (https://www.mk5golfgti.co.uk/forum/index.php?action=profile;u=3794)
I’m afraid to admit I became a bit disheartened with the situation. Although I still enjoy the car it really it is showing its age. Rusting , lacquer peel and now it’s on the daily school runs it steadily accumulating its dings too.
So apart from the above fiddling with the WG I have just let it be :sad1:
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Thank you for coming back on here and responding....I was curious if you had ever decided to upgrade the WG or at least have it inspected.
I know about having an unexplainable issue...where you have to replace $#!@t in a process of elimination. I still haven't sorted out why my fuel rail pressure only specifies 110 bar when it should be 140 bar. After more than two years of digging and working with GIAC, nothing. I can only assume, because I went from GIAC to DriverMotorsport(DM) to GIAC again. When I was using the DM tune, I did a couple of swaps. One being I added a Forge WG Actuator for the K04 because their tune was at 26 PSI and the stock WG Actuator was having trouble staying closed so to build the boost when added preload didn't help. The other was I went catless. So those two are my focus now. I plan to get a new K04 turbo and that will have the oem actuator...and then I am going to get another catted DP.
Anyhow, I was trying to help someone with a similar issue to yours. He recently had his 2006 GTI (w/K03) tuned, but it only boosts to 17 psi and tapers down to 10 psi. Still working with him and he says there are no leaks and the DV and N75 have been replaced. But I have yet to see his boost data which he promised soon. I am leaning on it being the WG is loose to not seal when shut, the WG actuator spring is not strong enough or it needs more preload.
Sad to hear yours has been on a rough road as of late...hope you have a pick-me-up soon. Mine is luckily been able to be driven less...approximately 2500 miles per year and it is still being garaged...but it is looking to need near $4000usd in parts soon. It's a long list. :confused:
This was a month ago...can't believe I have had it for near 13 years now.
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